My Explorer -project (2006-07-03)

Another carb check and new tank



One of this year vacation thing-to-do was to test the hovercraft and make it run.
 
Carb had caused some issues during latest operations and it was at some point removed and overhauled with new service kit. Previously it was just cleaned and put back together with silicone gasket and old gear. At some point during spring 2004 or 2005 (can't remember exatcly) tank developed a leak causing 40liters of gasoline spilled on the floor of my craft. Tank wasn't that good anyway so no harm there, but little worried about the long term effects of gasoline exposure. It was laying there for max. of two weeks. Stink of gasoline has gone away now.

 
Before actually starting with the new tank, i wanted to make sure service kit had improved the carburettor. It was gone through and checked so many times in past without finding anything that i was quite pessimistic about it. As a temporary test i bolted in the carb and all the fuel and vacuum lines and filled the cooling system. As a fuel tank we used just a canister with hoses going in and out so no longer trips or test were possible, but brief test could be done. Also intake air filter was missing at this point. Old one (allthough being washable variety) had suffered so much damage it could not be used anymore and being special order item replacement wasn't easy to obtain. Allthough lot of debris in the air small test turned out to be succesful. Engine responded quite well and i could take rpms up with playing with accel enrichment. Service kit seems to have helped. Next step new fuel tank.
 
I was planning to use plastic universal outboard type tank, but i have fuel gauge sender installed as well as i need fuel return line. These plastic tanks have just one built-in connector. I could live with smaller size by using two of them and switch them as needed. But this would make needed extra connections even more difficult. Being on vacation i had time to source supplies and put together a sheetmetal style tank i originally had with few enhancements. Original capacity was 120liters (~32gallons) but due to location of filler line could not be filled much over 70-80liters. Also it was a single chamber without splash plates. It was laying on the floor and most important of all it was just carbon steel without any painting at all. Fuel tank cap was located outside the craft so if there was a spill when filling it would not go inside the craft.

 
I wanted to lift the tank off the floor this time and therefore it needed to be smaller to fit under rear seat. I did weight my options between aluminium, stainless and carbon steel, but decided to go with carbon steel for easier welding. I could do that home where good aluminium weld or nice finish on stainless requires TIG weld and experienced welder - much more costs than material itself. Besides i didn't want to spend much money beacuse i could still not be sure if my craft would work properly under normal operation conditions.  These plates are sold in 1000x2000mm sheets and i wanted to minimize cutting. But due to limitations of folding tool used i had to make a compromise. I  was aiming for 80liters capacity, but ended up with ~62liters. I purchased 1,5mm carbon steel plate, cutted and folded it to form a box of 250x250x1000mm. Edges that were to be welded wera also folded to easier welding of end plates. I also made a smaller box: 45x150x150mm. This will be the pickup location for fuel line. I made couple of splash plates to be placed inside the tank to dampen fuel sloshing.

 
It took me couple of days to weld everything together, but welding time was few hours. One needs to weld small passes and let things cool to prevent warping.  I started by slowly welding the longest seam, forming 250x250x1000mm frame. I then measured center location and made a hole to bottom of the tank. Hole is placed so that welded edge of the frame is pointing up (old engineering wisdom: best weld is non-existing weld). Hole is as round as i could make with angle grinder, perhaps 100mm in diameter. I hammered edges down a bit and placed the smaller box on the bottom side of this hole. Analogy is that when fuel moves in the tank some of it always finds it's way to lowest point: the pickup tray. The way the hole and box are dimensioned causes majority of it also trapped there even if craft is tilted. Pickup tube is then placed lower in the tank. I don't remember having problems because of this, but it should help especially when running with less fuel.

 
After pickup tray was in place i welded in the splash plates. They are 150mm high and placed in middle of  250mm total height. Thinking back they could have been almost full height and only open 1-2cm at the bottom. There are two of them in the tank. Again, didn't experinece this as a problems before, but it's good to dampen sloshing to minimize pressure build-up. Next the fuel feed and return lines and fuel gauge sender. This was the only part i used form old tank. Previously fuel gauge sender unit was bolted to attachment plate with five 5mm screws to threaded holes, but since it was easy to modify i welded 6mm nut to take bigger bolts and more threads. I initially overtorqued one of the 5mm bolts, since attachment plates was only 3mm. Now i don't have to worry about that anymore. Since tank was now smaller i shortened the pickup tube accordingly made a hole on the top pf the tank and welded in the attachment plate. One of the reason i choose 1,5mm plate over original 1,0mm was easier welding. With 1,5mm i could use higher setting and have airtight seam at once, where with 1,0mm you have to watch burning through material much more carefully.

 
By far the biggest compromise was the filling cap location. Before it was outside the craft, now it's inside on the top of the tank. Had i taken one extra trip to hoverport to measure and douple check the hull i could have done it the proper way and make a neck for placing filling ouside. But since i wasn't  sure craft is going to work and all this had already taken couple of weeks already i didn't want to do that. I wasn't too keen on having those additionl weld seams there either, so i put an piece old motorcycle fuel tank with cap there.

 
After everything was welded together it was time to test. I thought of using soap water in the tank, but hesitated because pickup tray system that would trap some of that in the tank. I used compressed air and our yard pool instead. Blocking all the connections and feeding compressed air into the tank i could spot two leaks, and issues with filler cap. Not too bad compared to first tank - using thicker material paid off. I patched those two spots and they were OK in re-check. I tightened the cap connection a bit with smaller hammer and it helper some. But that connection must have been originally soldered to tank itself and welding it had burned that off. I tried to re-solder, but could get it clean enough for soldering. I  adjusted the welding machine bit and welded it around which seemed to have done the trick. Problem solved. There is still some leak from the cap, but tank never sees 5bar  pressure as with compressed air and replacement air has to go in somewhere. Next step is to have some sort of surface treatment.

 
Hot dip galvanizing was out of the question because of pickup tray and being sheetmetal box. Preferred method was to have it galvanised, but their pricing was just too much for this even if i were sure everything works after i install new tank not mention i still wasn't sure about that. Powder coating, not perhaps the best way, but most cost effective at this time. Could do five powder coated  tanks with the price of 1 galvanised. Unfortunately (or not?) their schedule delayd the project more. As it happens, i was to pick up the painted tank next day i realized (while in the sauna) that i eventually had forgotten to weld if legs to raise the tank off the floor. Too bad, but i thought i could use some wooden blocks there or add them and patch the painting. I called them the next day to ask when i could pick it up. They promised to do the same day because they had not done it yet. I did not realize it rigth away either we just agreed when it was ready to be picked up. But as soon as i hang up the phone i realized that this is the good chance to add the legs. I called them back and had my father pick up the tank on his way home from work. This was also better for them since the reason it was not painted yet was difficulty to have i hanging due to lack of suitable holes. This happened on friday so later same weekend added some flat bar to raise the whole thing 30mm higher. Also put some holes to these legs to bolt wooden blocks to raise it further. I left the the tank to powder coating shop next Monday and it was ready on Wednesday.